1983 Volvo 242DL 
<-- back to Kirk's Volvo Page
I bought this car in the summer of 1998 from a college aged kid
that wanted something newer. The car originally belonged to his
aunt and uncle. It had approximately 160,000 on the odometer.
At the same time that I purchased this car, I also looked at a
1980 242GT. If you've never seen one, they were a special model that
Volvo came out with 1978 - 80. They weren't any faster than regular
240's, but they had lots of suspension goodies.
I suppose the almost purchase of a GT made me subconsciously begin
to upgrade this DL.
Some of my upgrades were from junkyard acquisitions and some were
from ipd. ipd has conveniently
brought back some of the GT suspension goodies.
Picture of the car during trip to 1999 VSA East Coast National Meet in Asheville,
NC. (This is before I upgraded to the 5 spoke alloy rims).
Upgrades
Tachometer
This car came with the large clock on the dash. I switched the
car over to the large tach/small clock setup from junkyard parts.
Voltmeter
Balu Vandor
snatched a 50mm voltmeter off of some water-cooled VW
at a junkyard and I added it to the empty gauge hole under the small
clock. I wired it into a spot on the fuse box that is on whenever
the key is in either the I or II position.
Swaybars
Turbo sways from a junkyard
Rear Headrests (junkyard)
Large style airdam (junkyard)
15-inch Volvo 5 spoke alloys with Bridgestone RE71 205/55 ZR15's.
Bilstein struts/shocks
ipd (GT) strut tower reinforcement plates
ipd Stainless steel brake lines
ipd (GT) upper and lower chassis braces
ipd (Nissens) all metal three row radiator.
The Bilstein and Brakes story.
Summer 2001
As the car topped 200,000 miles, the shocks/struts were wore out
and the car was beginning to creak and groan during turning. I began
to make plans for some upgrades/repairs. Conveniently, I was soon to
receive my George Dubya Shrub Tax Rebate check and I knew that to do my
civic duty, I must stimulate the economy by spending my rebate on foreign
made auto parts.
The brakes had also gotten spongy, so I replaced the pads with
PBR pads from ipd. I did a 10 second inspection of the calipers
and decided the fronts were ok and the rears were in so so shape (rubber
dust boot-wise). The brake fluid was dark and cloudy, so I decided
to take the car in and have the brakes bled.
Well, this is East Texas and Volvos are pretty exotic in these
parts. Most brake shops wouldn't touch it or didn't want to put Castrol
LMA fluid in it. In fact, it was almost impossible to find Castrol
LMA fluid for sale around here. I finally found some at Pep Boys in
Tyler. One shop said they could bleed the car and then admitted they
didn't know how to do it, AFTER the car had been dropped off. Then
a tire shop in Tyler (that is very popular and came highly recommended),
Bill Day Tires, agreed to bleed the brakes if I provided the fluid.
$50.00 and a few hours later, the car was "proclaimed" ready.
The car felt a little better, but not great. Then within
a few weeks the brakes got much worse. The pedal would initially
give good pressure and then all at once the pedal would sink then firm
back up a bit. It was very predictable and repeatable.
I figured that the master cylinder probably had internal leakage.
I also noticed that the brake fluid was cloudy and dark again.
Not wanting to go through the bleed ordeal again, I purchased
an EZIBLEED pressure bleeder from ipd.
I had also ordered Bilstein Struts for the front and Bilstein
shocks for the rear.
So I was planning a big suspension and brake repair party.
For readers that don't know, some special tools are needed for
doing the front struts.
Top Nut Tool
Spring Compressors
Spanner Wrench to loosen the strut gland nut - can use a pipe
wrench
Ball joint separator/press
For things I plan on doing often, I purchase good quality tools.
Most of my tools are Craftsman.
For things I don't plan to do often, I am a firm believer in cheap
tools, such as Harbor Freight.
So I ordered a ball joint tool, spring compressors and spanner
wrenches from Harbor Freight.
The top nut of the strut holds
the strut piston to the upper strut mount bearing. The piston must
be held still with a wrench while the lock nut is removed. The nut,
however, sits deep inside of the bearing mount. The
Bentley manual faithfully shows the Volvo special tools required for
the job, while the Haynes manual quite innocently
shows the piston held by a regular open end wrench and the locknut being
turned by a deep offset box end wrench.
Problem: the locknut is a 24mm. Try finding a 24mm
deep offset box end wrench! (or a 15/16")
Every set of deep offset box end wrench set ends at 22mm or 7/8
in. (Actually I discovered one month after doing
this work that Craftsman does has a 15/16 deep offset box end wrench,
but when I visited the Sears in Tyler, I asked for a 24mm, which they
don't have - and didn't think to ask for the 15/16. Thinking
back - I probably had not run the calculation that 15/16 inches = 23.8125
mm.)
I search on the web and found that Snap-On makes a 15/16 wrench
which can be yours for a mere $50!!! ( The Craftsman wrench goes for
$22.50).
I splurged and ordered it.
It didn't fit. Not enough offset. (Look
at the picture again, the offset would have to be
nearly 90 degrees, and the Snap-On and Craftsman wrenches only feature about
a 60 degree offset.
So my boss, Brian Capps, using measurements we took off of the
car, fabricated a tool to do the job.
He sawed off a socket, welded on a plate and drilled a hole through the plate
so a wrench can hold the strut piston. Here is a view of
the tool sitting on top of a strut. Note
that there is just enough room to slip on a 10 mm wrench to hold the strut
piston steady.
In the meantime - while I was waiting for tools/parts to arrive
(and or be fabricated), I went ahead and did the rear shocks and started
to work on the brakes. I wanted to make sure the bleeder valves on
the rear calipers were in good shape while I had the rear of the car jacked
up.
Guess what... the valves were both broken off.
This means that Jim Day Tire of Tyler either broke off the bleeders
when they bled the lines or (more likely) they didn't bleed the brakes
at all and took my $50.
Since the rear rubber dust boots didn't look very good when I
replaced the pads earlier in the summer, I went ahead and ordered a pair
of rebuilt ATE calipers. And since I was going to be replacing the
calipers I went ahead and ordered ipd's stainless steel brake lines.
It helped that they were on sale.
I had also decided to paint the new calipers red.
When the calipers arrived, one of them was missing the bolt-on
bump stop. What is the exact purpose of the bump stop anyway?
It looks like it is there to limit the crumple of the trunk in an
accident. It also looks as though it would stop the crumpling
trunk from shearing off the brake lines in the rear. All-in-all
a pretty necessary piece of steel.
I painted the calipers and gathered all tools and parts and awaited
Labor Day Weekend 2001.
At this time, I don't really have a decent paved surface for working
on cars, so I loaded the trunk of the DL with every tool I could think of
possibly needing and a formidable arsenal of aerosol automotive chemicals
and headed to visit my parents who live just outside of Dallas, TX.
My Dad cleared the garage for me and we turned it into a impromptu Volvo repair
shop.
Day 1
The car went up on all fours and we began taking apart the front
suspension. This was the moment of truth for the "tool". After
several applications of PB Blaster pennitrant an attempt was made to free
the stuck strut top nut.
So much planning, tool searching, purchasing, fabricating had
been expended. All for naught - the nut wouldn't budge and we were
starting to round off the top of the strut. The 10mm open face wrench
was rounding off as well.
So we pulled off the entire strut and hub assembly. Before
loosening the three upper strut mounting nuts, I marked the suspension
setting like it shows in both the Haynes and the Bentley manuals.
I also had to remove the rotors and calipers. I went ahead and disconnected
the calipers because I was going to be putting on the stainless steel
brake lines. There is a good picture in the Haynes manual of the
three nuts you have to loosen to remove the control arm off of the A-arm.
You also have to separate the ball joints on the end of the steering rack
and to take off the ends of the front swaybar.
With the assembles removed, I used my spring compressors to widen
the gap of the coils at the point that the gland nut. The gland
nut hold the strut cartridge onto the strut tube. In my mad purchase
of cheap chinese tools, I had ordered a set of Spanner Wrenches, which
are perfectly designed to remove the gland nut. Typical with my experience
in this project, they didn't arrive until 3 weeks after I completed the
work. So I used a pipe wrench - 2 actually - one to turn the nut,
and one to hold the strut tube still. If you do this, and you have
the assembly laying on the ground, there will still be some compression
on the spring and the strut cartridge will eject out of the tube and travel
about 18 inches. So be careful.
The strut cartridge still had the seized top nut attached, with
the old upper strut mount bearing and the upper spring seat still attached.
I had new upper strut bearings, but I needed to reuse that upper spring
seat. So I called around and found a Firestone shop that agreed to
remove the top nut for me. They put an impact wrench on the nuts
and spun them off. All that special tool nonsense and it was as easy
as getting someone to do it with an impact wrench. Best of all they
didn't charge me! So here is a free plug for the nice guys at the
Firestone Shop on Camp Wisdom Road in Duncanville, Texas!
By the way, the old cartridges said "V O L V O" on them and were
probably the original cartridges - 18 years old!
This ended the work for the first day.
Day 2
On Day 2, we put the assembles back together with the new Bilstein
cartridges.
The cartridges were depressed once completely to distribute the
strut oil, per manufacturers instructions. Don't be surprised if
the struts act stubborn at first and don't want to compress. I put
a shop rag on the garage floor, inverted the tube and pressed down on the
cartridge.
I took a dab of the excess strut oil and smeared it on the threads
of the strut tube and on the Bilstein gland nut. Bilstein
supplies a special gland nut tool that indicates the proper torque
for the gland nut. Careful that ring tool wants to slip off
often!
Next the spring has to be compressed so the infamous top nut can
be put on. It is a slow, tedious, and exhausting process to crank on
the spring compressors until the top nut can be attached!
With the upper spring seat in place and the NEW upper strut mount
on top, it was time for the top nut torquing. Being obsessed
with the top nut removal for over a month, I had also been thinking
about it's subsequent replacement. Stock
struts (and some other brands) have threads that run up the piston
shaft so far and then the top is flattened on the side to accept a 10mm open
face wrench. The Bilsteins are threaded all the way to the top with
an 8 mm allen wrench hexagonal hole in the top of the strut.
Brian, my boss and inventor of the now infamous "tool", and I simultaneously
had a thought. Why not put a spacer under the top nut that lifts the
nut up enough that the special tool is not necessary? I went to Tractor
Supply ("Where America's Farmer's Shop" - it says) and found two shaft collars
that were about the height of the top nut and fit the strut piston shaft
without any play, but not too snuggly (pic of nut with
spacer). Here is a pic of the torquing
. With the spacer in place, the expensive Snap-On wrench fits nicely.
Trivial note: With the Snap-On wrench turning the nut clockwise, my torque
wrench had to turn the shaft counter-clockwise. I had to turn
the knob on the torque and torque counter-clockwise for the first time ever.
Look at the picture again and think about it, if
you aren't getting it.
With the top nut in place, the next step is probably the most
physically challenging.
I had to try to cram the assembly back into the strut tower and
get the three bolts on the upper strut mount to pop up through
the holes in the tower. It was sort of a 10 minute cram and
wiggle with this really heavy assembly while my Dad fiddled with putting
the nuts on. He just concentrated on getting each nut started.
I then went back one by one and reattached the nuts after adjusting the position
of the strut assembly to match the timing marks I had marked the day before.
I chose to add the ipd strut tower reinforcing plates. These sit on
top of the strut bearing and under the tower. I'm glad I didn't forget
them, or I'd have had to to the cram and wiggle for 10 more minutes!
I experimented with many different bizarre ways of trying to get
the control arm and the A-arm to line back up with little success.
I was concentrating on how to get the strut assembly and control arm to line
up with the A-Arm. But that means you have to compress the spring.
Then the 5 watt bulb in my head went off and I realized that
it is way easier to lift the A-arm and make it line up with the control
arm and the strut! 30 seconds later, bingo...
Another of my cheap Chinese tools was a Ball Joint Tool.
This monstrous thing that I got for little dough from Harbor Freight must
have been designed for working on diesel trains or something. I
had to jack up the assembly some to give this tool clearance, but it worked
at squeezing and holding the joint still so the nut can be attached.
Without pressure on it, the ball joint wants to freely rotate when you
turn the nut.
I then reattached the swaybar ends. This is an annoying
job to do solo. If you get one end attached, the other end gets jammed
up. I usually spend a lot of time running back and forth from one side
of the car to the other.
TA DA! suspension DONE!
End of Day 2 - We cleaned up and went to my niece's wedding.
Day 3
Remember, there was brake work to be done...
Since I had removed the front calipers in order to remove the
strut assemblies on Day 1, I took the brake lines off of the calipers and
painted these calipers red to match the rebuilt ones for the rear.
First I removed the old rear calipers and attached the stainless
steel brake lines.
Then I attached the rebuilt rear calipers.
In the cheap Chinese tool department, I thought I had really done
my homework. I had bought a set of Flare Nut Wrenches so I wouldn't
round off any brass fittings. It turns out that the 3 main sizes
of wrench needed for brake work on a Volvo are 8, 11, and 14mm.
My cheap set of flare nut wrenches didn't come with 8 or 11!
I attached the front stainless steel lines.
Then in my haste to attach the front calipers, I cross threaded
one of the brass fittings where it attaches to the caliper itself.
For hours, my dad and I carefully filed on the threads to try to reattach
the fitting.
BE VERY CAREFUL when messing with these fittings. Lesson:
Attach the fittings to the caliper by hand, backing out at the slightest
resistance. After it is hand tight, only then do you touch it with a wrench.
I gave up and assembled as much as I could of what was left to
do.
He fiddled and filed some more and then he gave up.
I repacked both front bearings with grease - almost leaving off
the cotter pin on one side (that would have made for a wild trip home!)
I wiped off my hands and walked over to the work bench and casually
attached the fitting on the first try!
Side note: It is tedious work getting the brass fittings
and the brake lines to want to mate. The threads are very fine and
neither fitting wants to be at the proper angle.
With everything attached, we gave up for the night.
Pics of painted calipers (and stainless lines/Bilsteins) -
right front - left front -
right rear
Day 4
Only thing left - New master cylinder and brake bleeding.
The master cylinder was a breeze, the fittings cooperated, etc..
I had purchased the ipd EEZI-bleed, the one that uses tire pressure
to feed the liquid so it is a one man job.
I followed the sequence in the Bentley Manual:
Left rear
Left front top chamber
Right front top chamber
Right rear
Right front lower chamber (both sides)
Left front lower chamber (both sides)
Left rear - lots of air and lots of dark fluid. so far so
good.
Left front top chamber - nothing. What? Nothing came
out. at all!
I bled the rest of the sequence in disbelief and tried it all
over again.
Same thing.
I disconnected the EEZI-Bleed and started the car (on the jack
stands) and tried the brakes.
NO PEDAL.
I felt like an idiot.
I replaced the rear calipers with rebuilt ones because the bleeders
were broken and the dust boots looked bad - I didn't even think about
the fronts being bad.
I removed the left front caliper and tried to blow through the
top chamber and nothing came out - it had a blockage.
Before doing any of this work, the pedal feel was week and I new
the fluid was old. That's why I had those criminals at that tire shop
in Tyler "bleed" the brakes. We know that they didn't.
I should have tested the calipers when I had them off doing the
suspension work.
I have a portable air compressor that I use for tire filling with
me. I attached the soccer ball needle and put it in the brake line
to the top chamber. Holding this connection as tight as I could, I opened
the bleeder valve and got the air pressure up to 100 psi and still couldn't
bust through the blockage. When I hooked the needle to the lower
chamber, it immediately moved the pistons.
It was getting late in the afternoon, so my Dad and I dashed off
to a nearby Dallas area junkyard - one that I had never been to before.
The one that I had been using was down to only 2 or 3 240's.
Well we hit the jackpot with the second place. I have found the Dallas
Volvo Valhalla - the great hereafter for Volvos! They had several rows
of 240's.
The tricky part was I needed a 240 with NON-VENTED front rotors.
Found one - squirted PB blaster on everything in sight and then
went sight seeing for a few minutes.
Came back, caliper bolts budged, but the brake lines wouldn't
separate. More Blaster...
Found 2nd Non-vented car. Someone had already removed the
brake lines... good... Blaster... caliper bolts budged...
removed caliper and set it on the hood of a BMW... (brake fluid
is good for beemer paint). Blaster on the bleeder valves...
no budge...
Back to 1st car... more Blaster... no budge...
Found 3rd car... Blaster...
Back to 2nd... more Blaster... bleeders no budge...
paint on beemer starting to run...
3rd car... caliper bolts budged... brake lines no
budge... explained to Dad why you can't just cut the lines - the fittings
are attached sandwiching the bracket. More Blaster...
Back to 1st car... more Blaster... no budge...
Back to 2nd... more Blaster... bleeders no budge...
Back to 3rd car... brake lines budge! removed caliper and
placed it on hood of a Saab. Blaster on the bleeders...
Back to 1st car... more Blaster... no budge...
Back to 2nd... more Blaster... bleeders no budge...
Back to 3rd car... Bleeders budge! I apply lips to brass
tubes and blow - brake fluid flies all down feeder of Saab (brake
fluid is good for Saab paint as well)! Pistons move when
I squeeze with fingers. WE HAVE A WINNER!
In between all this running around, I was taking inventory of
what I saw at the yard and it had several noteworthy cars including several
with the heavy 2-door Turbo trim that I want to put on may tan car and there
is even a 2 door 240 with BROWN interior, so I can replace my rotten door
panel.
Anyway - these things will have to wait for a later trip.
We went back to my parents house and I attached the caliper -
just as it starts sprinkling rain. I begin to hurry through a bleed
as it gets dark and I'm not too happy with the pedal feel - better but not
good.
(pic of junkyard caliper not painted)
I decide I need to stay one more day.
Day 5
Call into work and tell them I'm stuck in Dallas with no brakes.
Do another bleed - slowly, carefully.
Do a second bleed - slowly, carefully.
Here is a picture of all of the fluid collected
. The bottle on the right is from the final bleed and it is a
tiny bit cloudy from some Diet Coke that was still left in the bottle!
BTW: Castol LMA brake fluid is all I use.
Finally I have brakes. The pedal isn't as rock solid as
I have experienced in the past. Actually, no, that's not the problem.
The pedal feel is fine - it's the pedal travel - it travels an inch or
so further before you feel the brakes start to work. then they work
just fine. It's very predictable, but weird at first to get used
to. Since I have more than one 240, every time I switch cars,
the brakes feel funny, the acceleration is different, the clutches let
out differently, the seats feel different, etc... blah, blah, blah.
One the 2 hour ride home, I had the benefits of a full Bilstein
suspension and good brakes.
And 3 out of 4 painted calipers aren't so bad!
<-- back to top
<-- back to Kirk's Volvo Page